Good practices and investments related to Cleaner Production
Example No. 3
Reducing organic solvent emissions and elimination of hazardous waste
Company:
FAMED Żywiec sp. z o.o.
Industry branch: electrical machinery industry (manufacture of medical equipment)
Resources in question:
- Materials (paints)
- Chemicals (solvents, TRI)
- Emissions into the atmosphere (VOCs)
- Waste (hazardous)
Cost (implementation of good practice): Medium
The
company's manufacturing processes require that the surfaces of
manufactured parts be thoroughly cleaned before paint coatings are
applied on them. The technological processes used in the preparation and
application of paint coatings on parts were a source of negative
environmental impact – high emissions of volatile organic compounds into
the atmosphere and the generation of large amounts of hazardous waste.
Prior to modernization, steel parts were degreased in trichloroethylene
vapor. The volume of trichloroethylene emissions from this operation was
0.716 Mg/year, which translated into annual trichloroethylene
consumption of 1,500 liters.
The process of painting steel surfaces was a wet process, using phthalic paints. Annual consumption of paints (about 320 kg/year) and their solvents (about 340 kg/year), resulted in VOC emissions of about 0.490 Mg/year with single-shift operation.
The process of painting steel surfaces was a wet process, using phthalic paints. Annual consumption of paints (about 320 kg/year) and their solvents (about 340 kg/year), resulted in VOC emissions of about 0.490 Mg/year with single-shift operation.
Applied solution:
Modernization of the surface degreasing process prior to painting and installation of a modern powder coating plant.
Modernization of the degreasing process
As part of the modernization, the process of degreasing surfaces in trichloroethylene vapor (the so-called TRI washer) was replaced by degreasing operations in a Finnish washer and rinsing on a so-called washing line. These operations are carried out in aqueous, low-concentration and low-temperature preparations. The Finnish washer is a closed device and is not a source of environmentally harmful emissions. On the other hand, the washing process carried out in the washing line, where elements are washed, rinsed and passivated (temporary corrosion protection) results in negligible emissions of pollutants into the atmosphere (ethylenediamine 0.008 Mg/year).
Installation of a modern powder coating plant
The
wet painting process has been replaced by powder coating process. This
process does not emit pollutants into the atmosphere. In the paint shop,
components for hospital beds are painted: from the tiniest drive
systems to frames or beds measuring 200 cm by 80 cm. The paint shop,
operating in a single-shift mode, uses about 500 kg of powder paint per
month. Due to the nature of the product, very different paint surface
thicknesses are required: from 70 to 500 µm. The paint shop uses a
cyclonic powder recovery system based on a double cyclone, ensuring very
high efficiency in powder paint recovery. The separated powder is
returned to the process. The paint line is an efficient machine,
operating at speeds of up to two meters per minute.
Changes in technological processes related to the application of paint coatings involved:
- Replacement of wet painting with powder coating, implemented between 1995 and 2001.
- Elimination of organic solvents from the sheet metal pre-washing process – 1999.
- Elimination of trichloroethylene from sheet metal washing operations prior to powder coating – 2001.
Obtained benefits and effects of the implementation:
- Reduction in emissions of volatile organic compounds by about 80%
- Reduction in the amount of hazardous waste requiring disposal by approximately 96%
- Improvement of health and safety conditions at workplaces
- Reduction of paint shop operating costs
Paint shop after modernization
photo by: FAMED Żywiec sp. z o.o.
Sources:
- “Sustainability Reports” submitted by FAMED located in Żywiec as part of the Polish Cleaner Production Movement
- Materials submitted by FAMED Żywiec Sp. z o.o.
This
material has been subsidized by the National Fund for Environmental
Protection and Water Management. The Polish Cleaner Production Movement
Association is solely responsible for its content
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